Wednesday, December 28, 2011

Ashtabula River Railroad Disaster

December must have been the time for bridge collapses in the 1870's

December 29, 1876:
The Ashtabula River Railroad Disaster (also called the Ashtabula Horror or the Ashtabula Bridge Disaster) was a train disaster caused by bridge failure. It was, at the time, the worst rail accident in American history (succeeded by the Great Train Wreck of 1918) when it occurred in far northeastern Ohio on December 29, 1876, at 7:28 p.m.
One or perhaps two of the bridge designers later committed suicide. The disaster helped focus efforts to draw up standards for bridges including adequate testing and inspection.
The bridge, designed jointly by Charles Collins and Amasa Stone, was the first Howe-type wrought iron truss bridge built. Collins was reluctant to go through with building the bridge calling it "too experimental."
The Lake Shore and Michigan Southern Railway Train No. 5, The Pacific Express, left a snowy Erie, Pennsylvania, on the afternoon of December 29, 1876. As The Pacific Express plowed through the snow and crossed a bridge over the Ashtabula River, about 100 yards (90 m) from the railroad station at Ashtabula, Ohio, the passengers heard a terrible cracking sound. In just seconds, the bridge fractured and the train plunged 70 feet (21 m) into the water.
The lead locomotive "Socrates" made it across the bridge, while the second locomotive, "Columbia" and 11 railcars including two express cars, two baggage cars, one smoking car, two passenger cars and three sleeping cars and a caboose fell into the ravine below, then igniting a raging fire. The wooden cars were set aflame by kerosene-heating stoves and kerosene burning lamps. Some cars landed in an upright position and within a few minutes small localized fires became an inferno.
The rescue attempt was feeble at best because of the ill-preparedness of the nearby station to respond to emergencies. Of 159 passengers and crew on board that night, 64 people were injured and 92 were killed or died later from injuries sustained in the crash (48 of the fatalities were unrecognizable or consumed in the flames). It is unclear how many died of the fall, separate from the blaze. Matters were made worse by the heavy snow the area had just received.
Some recent authors have attributed the accident to fatigue of the cast iron lug pieces which were used to anchor the wrought iron bars of the truss together. Many were poorly made, and needed shims of metal inserted to hold the bars in place.
One good thing about engineers is that they generally investigate why things fail so that they can avoid the mistakes in the future.  I wonder if the cold weather played a part in the Tay Bridge disaster and this one?

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